Re: Charging system question
Posted: Wed Nov 06, 2013 4:11 am
Well, I still don't know what was wrong with the charging system but it is working as-designed as of today. The connections were all checked and then another diagnostic was run on the system.
To test the alternator output, the field was connected directly to the hot bus which bypassed the controller.The engine was then run while monitoring the output current and voltage. Both remained steady at steady load and rpm and both varied directly with load and rpm which confirmed the alternator was operating properly.
Then the system wiring was returned to normal and the engine restarted. The alternator charged properly and continued to load and unload as system loads were added and removed. The plane was then flown trying to duplicate the previous flight's problems with the current fluctuating. During the entire flight, the voltage remained at 14.3 and the current was a consistent +1 or +2amps which is normal.
So, we still don't know what caused the problems but connections were probably the culprit. Nothing was done to any other part of the system and it went from not working at all, to working erratically, to working properly by just removing and reattaching connections. It remains to be seen if the problems will reoccur but if they do, we'll start over and figure it out. At least I have a better understanding of how the system works now.
To test the alternator output, the field was connected directly to the hot bus which bypassed the controller.The engine was then run while monitoring the output current and voltage. Both remained steady at steady load and rpm and both varied directly with load and rpm which confirmed the alternator was operating properly.
Then the system wiring was returned to normal and the engine restarted. The alternator charged properly and continued to load and unload as system loads were added and removed. The plane was then flown trying to duplicate the previous flight's problems with the current fluctuating. During the entire flight, the voltage remained at 14.3 and the current was a consistent +1 or +2amps which is normal.
So, we still don't know what caused the problems but connections were probably the culprit. Nothing was done to any other part of the system and it went from not working at all, to working erratically, to working properly by just removing and reattaching connections. It remains to be seen if the problems will reoccur but if they do, we'll start over and figure it out. At least I have a better understanding of how the system works now.